Hello all,
Well, after a nice weekend on the water, a minor setback.
My 8hp Honda is a 2004, purchased this year with about 100 hours on it. The dealer stated in the ad that the impeller was changed before sale, and the motor has run well since I've had it. I used it as recently as yesterday for trolling, for something like an hour--it would have overheated if it wasn't getting water.
It has always been a bit hard to get a solid stream out of the telltale with earmuffs, but possible. Today, I was having a heckuva time flushing it with the muffs, and eventually submerged the lower unit in a bucket of water instead. Still no water, but some steam. Not a good sign.
I started to pull the lower unit, but thought I'd check inside the intake screens first. In there, I found bits of rubber that account for 3-4 fins from the impeller, so at least that mystery is solved. I also noticed that 2 of the 5 lower unit bolts are missing, and the others have blue loctite on them. So, either the mechanic forgot the loctite on the other two, or forgot the bolts.
In fairness, I have forgotten a time or two to turn on the earmuff water until after starting, i.e. start the motor, say "Oh S--t!", jump out of the boat, turn on the water.
So--did the impeller fail because it wasn't replaced, because it overheated due to lack of water, or something else I haven't thought of yet? The missing bolts really make me suspect of the quality of the labor, but also wanting to be fair about this.
Lastly, the Heloc manual calls for the shift linkage to be removed up top in order to remove the lower unit. The description makes it sound like a pin, with a straight shaft. My linkage is bent 90 degrees at the top, and I have a hard time imagining that part going through the case--can someone reassure me that it will indeed pass through once the grommet is out of the way?
Thanks and talk soon.
bmc
Well, after a nice weekend on the water, a minor setback.
My 8hp Honda is a 2004, purchased this year with about 100 hours on it. The dealer stated in the ad that the impeller was changed before sale, and the motor has run well since I've had it. I used it as recently as yesterday for trolling, for something like an hour--it would have overheated if it wasn't getting water.
It has always been a bit hard to get a solid stream out of the telltale with earmuffs, but possible. Today, I was having a heckuva time flushing it with the muffs, and eventually submerged the lower unit in a bucket of water instead. Still no water, but some steam. Not a good sign.
I started to pull the lower unit, but thought I'd check inside the intake screens first. In there, I found bits of rubber that account for 3-4 fins from the impeller, so at least that mystery is solved. I also noticed that 2 of the 5 lower unit bolts are missing, and the others have blue loctite on them. So, either the mechanic forgot the loctite on the other two, or forgot the bolts.
In fairness, I have forgotten a time or two to turn on the earmuff water until after starting, i.e. start the motor, say "Oh S--t!", jump out of the boat, turn on the water.
So--did the impeller fail because it wasn't replaced, because it overheated due to lack of water, or something else I haven't thought of yet? The missing bolts really make me suspect of the quality of the labor, but also wanting to be fair about this.
Lastly, the Heloc manual calls for the shift linkage to be removed up top in order to remove the lower unit. The description makes it sound like a pin, with a straight shaft. My linkage is bent 90 degrees at the top, and I have a hard time imagining that part going through the case--can someone reassure me that it will indeed pass through once the grommet is out of the way?
Thanks and talk soon.
bmc